Re: Help Please. 11 inch brake upgrade gone bad. Reply #45 – April 04, 2021, 09:10:14 PM They are not needed when switching to the 87-93 style spindle for the 11” brakes.
Re: Help Please. 11 inch brake upgrade gone bad. Reply #46 – April 04, 2021, 11:48:52 PM Going to be a bear to drive to the alignment shop like that.You should get it close(r) to neutral before trying to drive it. Tie rods might be a kind of a pain if they haven't been touched in a while. Last Edit: April 05, 2021, 08:34:08 AM by Chuck W
Re: Help Please. 11 inch brake upgrade gone bad. Reply #47 – April 05, 2021, 09:49:24 PM going to half ass align it with string method before going to the shop; either that or flatbed it...not going to wreck my new BFG's lol. Also have new tie rod ends for it on the way, no reason not to at this point. 1 Likes
Re: Help Please. 11 inch brake upgrade gone bad. Reply #48 – April 05, 2021, 10:39:05 PM Just to clarify, did you loosen the LCA bolts and reset the bushings with the suspension loaded? Would hate for you to spend the $$$ on the alignment and have it fall out later if they were preloaded. Not saying it would happen but again, it’s free. 1 Likes
Re: Help Please. 11 inch brake upgrade gone bad. Reply #49 – April 11, 2021, 07:26:08 PM Problem appears to be solved, gentlemen. I set the toe with a string and test drove it, it was fine; took it for a full alignment, its all good now. The camber DID have to be set all the way all the way in on the shock towers, though. Like I said before, apparently the toe being way the hell out, like it was when I finished the installation, was forcing the camber out when i drove it out of the garage, then pulling it back in when I backed it back in. No, there was no problem with the steering rack or tie rods, and my control arm bushings are not seized. 3 Likes
Re: Help Please. 11 inch brake upgrade gone bad. Reply #50 – April 11, 2021, 11:03:10 PM Well, I did mention that the Fox chassis wants to add positive camber to the outside wheel when turning. With it toed in that bad, I'm sure it added a lot of camber to it. It's going to scrub pretty badly going forward to backwards like that.The bushings were a guess, but it didn't sound like you'd lowered the control arm enough for that to be an issue.Glad it's sorted.